AGMA 99FTM11-1999 Performance of Nitrided Gears in High Speed Epicyclic Gearbox Used in Gas Turbogenerators - a Case Study《燃气轮机发电机组用高速行星齿轮箱中的氮化齿轮的性能.一项案例分析》.pdf
《AGMA 99FTM11-1999 Performance of Nitrided Gears in High Speed Epicyclic Gearbox Used in Gas Turbogenerators - a Case Study《燃气轮机发电机组用高速行星齿轮箱中的氮化齿轮的性能.一项案例分析》.pdf》由会员分享,可在线阅读,更多相关《AGMA 99FTM11-1999 Performance of Nitrided Gears in High Speed Epicyclic Gearbox Used in Gas Turbogenerators - a Case Study《燃气轮机发电机组用高速行星齿轮箱中的氮化齿轮的性能.一项案例分析》.pdf(6页珍藏版)》请在麦多课文档分享上搜索。
1、- 99FTMllPerformance of Nitrided Gears in HighSpeed Epicyclic Gearbox Used in GasTurbogenerators - A Case Studyby“ A.K. Rakhit, Gear ConsultantAmerican Gear Manufacturers AssociationTECHNICAL PAPERPerformance of Nitrided Gears in High Speed EpicyclicGearbox Used in Gas Turbogenerators - A Case Study
2、Dr. Ajit K. Rakhit, Gear ConsultantThe statements and opinions contained herein are those of the author and should not be construed as an official action oropinion of the American Gear Manufacturers Association.AbstractHigh speed epicyclic gearboxes used in gas turbogenerators are typically designed
3、 with either carburized and hardened ornitrided gears. Each of these types of gear has its own merits and limitations. While carburized and hardened gears offeroptimum design, nitrided gears are sometimes preferred because of their low heat-treat distortion. In terms of loadcapacity, carburized and
4、hardened gears perform satisfactorily not only under steady load but also heavy shock load.Nitrided gears, on the other hand, are known to operate successfully only under steady state load. The fatigue life of thesegears reduces significantly under heavy shock load. That there is also aconsiderable
5、reduction of nitrided gears life underrated load with wide fluctuations is unknown. A recent failure of an epicyclic gearbox with nitrided gears that wasoperating under such loading confirms this fact. In this case, the gearbox was used to reduce the speed of a gas turbinerated 10.4 roW. During the
6、engine wash cycle, the load at the generator end varied from 0 to 10 mW at 1.5 cycles persecond for about 25 seconds duration, with the peak occasionally reaching to 12 mW. No such failure is reported insimilar gearboxes that are operating at various installations that did not experience this type o
7、f load fluctuations.Copyright 1999American Gear Manufacturers Association1500 King Street, Suite 201Alexandria, Virginia, 22314October, 1999ISBN: 1-55589-749-5,AVPERFORMANCE OF NITRIDED GEARS IN HIGH SPEED EPICYCLIC GEARBOXUSED IN GAS TURBOGENERATORS m A CASE STUDYA. K. RakhitGear ConsultantLaguna N
8、iguel, CaliforniaIntroduction FailureIncidentCase carburized and hardened gears are known to operate According to a field representative, gearbox failure occurredsatisfactorily both under steady and overload conditions, after three hours of operation following a scheduled on-lineNitrided gears, on t
9、he other hand, seem to perform well only turbine water wash cycle. In general, all turbines go through aunder steady load 1. Shock loads detrimentally affect nitrided water wash cycle after a few thousand hours of operation.gears life 2. Thus, nitrided gears are rarely used in applications During su
10、ch a cycle for this turbine, the generator load is broughtthat experience occasional shock loads. However, that the life of down to about the 80 percent level and then water is injectednitrided gears may also deteriorate when subjected to a rated load through the compressor section of the turbine. F
11、ollowing wash,that varies widely in a very short time period is relatively the load is raised to the maximum continuous level. After theunknown. Although, such load spectrmns are not very common, last wash cycle, high vibration levels of the gearbox weresometimes these are observed in gas turbogener
12、ator applications, reported just before the gearbox failed. Unforamately, no dataAn analysis of a gas turbogenerator load during start-up shows were taken. The gearbox had a total of about 16,000 hours ofload fluctuations to occur whenever the fuel control system service before the failure.malfuncti
13、ons. In this paper, a case-study on the failure of Following tiffs incident, to ensure the failure was not causednitrided gears used in a gearbox subjected to a load with wide bymisalignmentofequipment or any malftmction ofcomponentsfluctuationsis presented, such as bearings, couplings, shaft, a tho
14、rough inspection wasconducted. The equipment alignment of the package was foundFailed Gearbox to be within the allowable tolerance. Also, no visible damage ofany component was noticed. This led the inspection toward theThe gearbox is of star epicyclic configuration and is used as gearbox internal co
15、mponents.a speed reducer in between a 10.5 mW gas turbine and an electric Visual inspection of the disassembled gearbox revealedgenerator. The general characteristics of the gearbox are: severe mechanical damage to all gears. The failure was socatastrophic that one complete tooth fell off from one o
16、f theHorsepower rating (hp) “ 16,500 planet gears and was found at the bottom of the housing. FigureInput speed (rpm) 8625 1 shows the damaged planet gear and Figure 2 the severed tooth.Output speed (rpm) 1,500 Tooth debris was noticed in various gear meshes. No abnormaldistress was found on planet
17、sleeve bearings, although the thrustThe sun pinion and planet gears are nitrided whereas the faces of output shaft sleeve bearings were completely wiped out.ring gear is just through-hardened. The design life of the gears Also, sealing surfaces of output shaft and labyrinth seal wereis 100,000hoursm
18、inimum, foundto beburnt.Ito.Figure 1 - Overall View of One Damaged Planet Gear Figure 3 - Detail View of the Received FragmentFrom the Failed tooth. Arrows indicatethe crack propagation direction Mag: 4XFigure 2 - View of Dislocated ToothTo determine if there were any discrepancies with the qualityo
19、f gear material and heat treatment, detailed metallurgicalevaluation was carried out with a section from the failed tooth.Metallurgical EvaluationFigure 4 - SEM View of the Fracture Surfaces of theExamination of the fragmented tooth revealed some well- Gear Fragment. Mag: 100Xdefined beach marks (Fi
20、gure 3) suggesting a typical fatiguefailure. The tooth segment was also analyzed by EnergyDispersive X-ray Spectroscope (EDS) and examined with aScanning Electron Microscope (SEM). The primary fracturesurface was relatively flat and showed well-defined crack growthmarks as illustrated in Figure 4. F
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