REG NASA-LLIS-1512--2005 Lessons Learned - Quench Module Insert (QMI) Furnace Type C Thermocouple (TC) Assembly and Testing Lessons Learned.pdf
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1、Lessons Learned Entry: 1512Lesson Info:a71 Lesson Number: 1512a71 Lesson Date: 2005-01-01a71 Submitting Organization: MSFCa71 Submitted by: Donald DugalSubject: Quench Module Insert (QMI) Furnace Type C Thermocouple (TC) Assembly and Testing Lessons Learned Abstract: The QMI furnace required custom-
2、designed Type C Thermocouples (TC) to meet the scientific requirements for the hardware. In implementing the custom requirement set and associated verification testing for these TCs notable anomalies/problems were encountered in two areas. The primary problem was the discovery of contamination (most
3、ly Carbon deposits) on the inner surfaces of the TC that led to acceptance test failures. A secondary problem was caused by attempting to maximize the TC wire size yet limiting the overall TC sheath diameter leading to assembly problems of each TC.Description of Driving Event: The QMI furnace requir
4、ed custom-designed Type C Thermocouples (TC) to meet the scientific requirements for the hardware. In implementing the custom requirement set and associated verification testing for these TCs notable anomalies/problems were encountered in two areas. The primary problem was the discovery of contamina
5、tion (mostly Carbon deposits) on the inner surfaces of the TC that led to acceptance test failures. This problem occurred during the calibration phase of the TC acceptance testing and specifically when the TC was brought up to operating temperature (900degC for this application) and temperature held
6、 for stabilization and data gathering. The start of the deposits most probably began at a lower temperature (400degC) and began to build up so that isolation resistance failed test specifications. Investigation led to the conclusion that the Alcohol-based cleaners used on each of the piece parts (sh
7、eath, insulator, wire) making up the TC was to blame. The Alcohol-based cleaners left deposits on some materials and were absorbed into the insulators. When the assembled TC was brought up to temperature during calibration testing the Alcohol-based substance was baked out and a Carbon residual remai
8、ned which was conductive.Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-A secondary problem was caused by attempting to maximize the TC wire size yet limiting the overall TC sheath diameter leading to assembly problems of each TC. The assembly of ea
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