AGMA 04FTM10-2004 The Failure Investigation and Replacement of a Large Marine Gear《大型船用齿轮的故障调查和更换》.pdf
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1、04FTM10The Failure Investigation and Replacementof a Large Marine Gearby: P. Hopkins, UK MOD Defence Logistics Organisation, B.A. Shaw,University of Newcastle, J. Varo, David Brown Textron, A. Kennedy, UKMinistry of DefenceTECHNICAL PAPERAmerican Gear ManufacturersAssociationThe Failure Investigatio
2、n and Replacement of a LargeMarine GearP.Hopkins,UKMODDefenceLogisticsOrganisation,B.A.Shaw,UniversityofNewcastle,J.Varo,DavidBrownTextron,A.Kennedy,UKMinistryofDefenceThe statements and opinions contained herein are those of the author and should not be construed as anofficial action or opinion of
3、the American Gear Manufacturers Association.AbstractFollowing a routine inspection of HMS INVINCIBLEs main propulsion gearboxes, cracking was identified onthe starboard main wheel teeth. This article presents a summary of the subsequent work, including: thepalliativerepair,inspectionregime,riskreduc
4、tionmeasures,failureinvestigation,thedesignandmanufactureof replacement gears and the permanent repair.Copyright 2004American Gear Manufacturers Association500 Montgomery Street, Suite 350Alexandria, Virginia, 22314October, 2004ISBN: 1-55589-833-51The Failure Investigation and Replacement of a Large
5、 Marine Gear P. Hopkins Marine Propulsion Systems IPT, Warship Support Agency, UK MOD Defence Logistics Organisation B. A. Shaw Design Unit, University of Newcastle, UK J. Varo David Brown Textron,UK A. Kennedy UK Ministry of Defence, Graduate Engineer Introduction The three Carrier Vertical Strike
6、(CVS) platforms in service with the UK Royal Navy (RN) provide the platform and facilities for the command and control of maritime and joint forces. They are 209m in length, displace 22,000 tonnes and have a complement of 685 ships company and 386 Air Group personnel. Powered by four 18MW Olympus ga
7、s turbines, they are capable of 28kts (see Figure 1). The CVS class was originally designed to carry large numbers of anti-submarine helicopters and to be protected from air attack by the Sea Dart weapons system. Sea dart has now been removed and the flight deck extended to increase the space availa
8、ble for parking aircraft. These versatile ships now deploy regularly with RAF Harrier GR7 strike aircraft aboard, as part of a mixed air group that can be tailored to operational needs. Air groups also include Sea Harrier FA2s, providing air defence, Sea King, Merlin and Chinook helicopters. With th
9、ese capabilities, the high value of the CVS platform has been demonstrated in many events since the 1980s. Figure 1 - HMS Invincible. Figure 2 - CVS Gearbox during build. Each CVS is fitted with two main propulsion gearboxes, the largest and most complex in RN service, designed and manufactured by D
10、avid Brown, now part of the Textron group. The triple reduction, reversing, double helical tandem design transmits power from either one or two Olympus gas turbines to a fixed pitch propeller. Manoeuvring ahead and astern is achieved by means of fluid couplings and for high power ahead operation dri
11、ve 2Figure 3 Flank pitting on a cracked tooth. is transmitted through two SSS clutches. The gearbox weighs 170 tonnes and contains 19 gear elements, the largest being the main wheel, which is 3m in diameter and weighs 22 tonnes (see Figure 2). In December 1999, during the Chief Engineers supercessio
12、n inspection of HMS INVINCIBLEs stbd gearbox, ships staff identified damage to a number of teeth on the main wheel. A full dye penetrant non-destructive examination (NDE) of the main wheel by David Brown revealed cracks originating from surface pits in 11 teeth. These varied in length up to a maximu
13、m of 30cm - see Figure 3. Palliative Repair Following an initial assessment it was decided to remove the cracks by in-situ dressing, to establish the full extent of the problem and to prevent any further crack growth. An iterative process of grinding and NDE was undertaken, to ensure that no crack i
14、ndications remained (see Figure 4). This resulted in the removal of 9 complete teeth and parts of 2 teeth (see Figure 5). Figure 4 NDE whilst removing a crack. Figure 5 Dressing to remove tooth sections and areas of pitting. A full and detailed inspection of the port main wheel revealed no defects c
15、onfirming that the problem was isolated to the starboard main wheel. Reducing the Risk of Further Damage It was clear that revised propulsion limitations were required if the risk of further gear tooth failures or deterioration was to be minimised. Therefore, to reduce the loads being experienced by
16、 the 3damaged main wheel teeth, revised single and twin engine torque limits were calculated, based on the loss of tooth contact area and an assessment of the allowable stress to theoretically assure infinite life. For the undamaged gearbox the torque at which additional engines were brought on-line
17、 (change-up criteria) was reduced, to avoid maximum tooth stressing at intermediate ship speeds. Whilst this did increase engine running hours and fuel consumption, it provided a margin of error against failure. The original twin engine maximum limitation was retained, but for urgent operational use
18、 only and a lower routine operational maximum was introduced to reduce the risk further. A revised procedure was also introduced to ensure that a good balance of torque was achieved between the Olympus gas turbines, particularly at high torques. With the torsion meter measuring output torque at the
19、main shaft, it had been possible for one engine to be working harder than the other, effectively overloading the main wheel teeth, but for this to go unnoticed because the total shaft torque was within limits. With these revised limitations and the close control of transients, the risk of further to
20、oth failure was assessed as small, but the ship was still able to meet her operational requirements. Subsequently a monitoring system was installed, which captured torque readings on a continuous basis, to enable the cause of any transients to be investigated and avoided. Monitoring the Defects To p
21、rovide early warning of any further deterioration, an enhanced inspection regime was devised. The defects were initially monitored following post repair trials and then by a rigorous three monthly inspection, undertaken using dye penetrant NDE by a specialist team consisting of MoD, David Brown and
22、Design Unit. Other monitoring techniques, including vibration analysis, were considered, but in tests this had not been able to reliably identify and trend deterioration. It was considered that new cracks would not propagate at a rate that would not be identifiable by the imposed regime of dye penet
23、rant NDE. The task of full scale dye penetrant inspection on a large wheel is time consuming and unpleasant to carry out, but it was felt that this technique gave the best opportunity of providing full coverage of all teeth with good accuracy for identification and monitoring of the crack types know
24、n to be forming. Although other methods are available for crack detection (e.g. ultrasonics and eddy current), these were not as easy to apply with confidence in-situ. Being a relatively simple technique to apply, dye penetrant was also made available as a backup during ships staff visual inspection
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