REG NASA-LLIS-6816-2012 Lessons Learned Space Transportation System (STS)-133 External Tank (ET)-137 Intertank (IT) Foam Crack and Stringer.pdf
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1、Public Lessons Learned Entry: 6816 Lesson Info: Lesson Number: 6816 Lesson Date: 2012-6-7 Submitting Organization: MSFC Submitted by: Jennifer Stevens Subject: Space Transportation System (STS)-133/External Tank (ET)-137 Intertank (IT) Foam Crack and Stringer Abstract: Thermal Protect System (TPS) f
2、oam cracking on the ET was discovered during the STS-133 post-drain walk-down after the scrubbed launch attempt on November 5, 2010. An investigation was conducted to determine the root cause of the stringer cracks and corrective actions to return the ET IT to flight status. The root cause was deter
3、mined to be the result of a failed aluminum-lithum (Al-Li) stringer, an element of the exterior metal surface of the Intertank. Description of Driving Event: During the Space Transportation System (STS)-133 post-drain walk-down following the November 5, 2010 scrubbed launch attempt, an anomalous the
4、rmal protection system (TPS) crack was observed in the External Tank (ET)-137 insulation, adjacent to the intertank (IT) to liquid oxygen (LOX) tank flange. The TPS crack was subsequently determined to be the result of a structural failure of the underlying aluminum-lithium (Al-Li) 2090-T83 stringer
5、. Later inspections detected a total of five cracked stringers. The investigation determined that the cracks originated along the bottom of the stringer feet through combined failure in multiple linked initiation locations. Failed stringer fractographic analysis indicated no pre-existing material de
6、fects, although a wavy refractive pattern that was not a surface contour condition was noted on the two lots of stringers prone to cracking. Other lots of stringers did not have the wavy pattern. The investigation determined that the material had low fracture toughness due to a microstructure evolut
7、ion process, termed recovery, which occurred prior to stringer processing (i.e., material processes were changed prior to stringer processing). Recovery in the two affected lots resulted in material with higher yield and ultimate stresses, and lower fracture toughness (i.e., more brittle). The time
8、of stringer/TPS crack occurrence suggested a thermally induced load contribution to the structural failure. The stringers were subject to assembly strains caused by initial installation on the IT panel as well as other mechanical events. Transient thermal loading occurs as the LOX tank fills prior t
9、o launch. All configurations tests exhibited high plastic hoop strains in the stringer feet due to the transient thermal loading, especially at the first three fastener locations. Cryogenic shrinkage during tanking causes rotation of the IT flange radially inward, which loads the IT stringer feet. A
10、nalysis suggests that the strain levels in the first three fasteners/bolt holes remain sufficiently high that a failure may occur. The bounding loading event is thermal loading. Analysis confirmed that installation of radius blocks over fasteners 2 through 7 reduces the peak hoop strain for the oper
11、ational loading events, but that they have a minimal effect on the assembly strain at fastener 1. During the investigation, the history of the implementation of Al-Li use in the ET was evaluated, including selection criteria, programmatic goals, and technical assessment review. Schedule and budget c
12、oncerns drove the ET Project to seek technical ways to significantly reduce the weight of the ET early in the Space Shuttle Program (SSP). In 1993, the ET Project was tasked with reducing ET weight by 10% in 48 months or less. Earlier, the weight was reduced from the Standard Weight Tank (SWT) to th
13、e Light Weight Tank (LWT; 1983-1998) by eliminating the paint, redesigning the feed system, and reducing margin of safety requirements on structural and load bearing parts wherever possible (i.e., Factor of Safety was reduced from 1.4 to 1.25 where possible). For the Super Light Weight Tank (SLWT),
14、the primary methods for reducing weight include use of Al-Li, a lighter, stronger replacement for aluminum-copper alloys, new welding techniques, and an orthogrid structure. Although Al-Li 2195 material cost 2 1/2 times that of the Al-Cu 2219 alloy used in the LWT, the weight savings were significan
15、t enough to justify the replacement. In addition, some areas of the ET that had low Factors of Safety were able to be modified to increase margins because of overall weight savings. The IT design verification included a combination of tests and analyses. To mitigate potential tank buckling concerns,
16、 designers maintained the structural ringframe stiffness, thrust panel material, and solid rocket booster (SRB) crossbeam design. Many of the subsystems, such as the skin stringer/joint interface, the beaded web, and the thrust panel, were tested to failure. The skin stringer/joint was improved to m
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