ASHRAE OR-16-C005-2016 Hot Gas Bypass Defrosting Strategy for Residential Heat Pump.pdf
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1、Hot Gas Bypass Defrosting Strategy for Residential Heat Pump Song Li Dennis Nasuta William Hoffman Associate Member ASHRAE Associate Member ASHRAE Ron Domitrovic, PhD. John Bush Cara Martin Member ASHRAE Member ASHRAE Associate Member ASHRAE ABSTRACT This paper describes a single-circuit hot gas byp
2、ass defrost strategy, similar to those used in commercial refrigeration applications, for a residential heat pump. Conventional heat pump systems defrost the outdoor coil by temporarily reversing the direction of the cycle such that the indoor unit acts as an evaporator and the outdoor unit acts as
3、a condenser, which dissipates heat to melt frost from the surface of the coil. This requires that the heat pump temporarily ceases to heat the home and actually uses the indoor coil to extract heat during defrosting. The hot gas bypass strategy does not require a reversal of the cycle, but instead b
4、ypasses some hot gas from the compressor discharge line through some or all of the circuits of the evaporator (outdoor unit) coil to remove frost. Similar defrosting strategies are successfully utilized in large-scale refrigeration systems such as those used in supermarkets, but these methods are no
5、t commonly implemented in smaller systems for the residential or light-commercial markets. A prototype system was developed for investigation consisting of a manifold system that allows hot gas to be bypassed from the compressor discharge line through any or all of the five circuits on the outdoor u
6、nit coil. Following the construction of the prototype system, proof-of-concept laboratory testing of the heat pump was carried out. Experimentation confirmed the capability of the hot gas defrosting strategy and provided initial quantitative results of the impact on system performance and energy con
7、sumption. The prototype has the capability to maintain partial heating capacity in the conditioned space while simultaneously defrosting the outdoor unit; this can be a substantial advantage over conventional systems. Hot gas bypass defrosting configurations of this type could make heat pumps a more
8、 attractive option to many users deterred by the limitations of conventional reverse-cycle defrosting. INTRODUCTION The concept of hot gas defrosting is common and successfully utilized in larger systems, including commercial refrigeration systems, but this approach has not been fully evaluated for
9、residential and light commercial heat pumps. A commercially-available 2.5-Ton (30,000 Btu/hr or 8.8 kW), 13-SEER residential heat pump system was modified and instrumented for experimental evaluation of a hot gas bypass (HGB) defrosting technique. The prototype system Dennis Nasuta and Song Li are T
10、hermal Engineers at Optimized Thermal Systems (OTS), Inc. in College Park, MD. William Hoffman is an Experimental Technician and Cara Martin is the Engineering Manager at OTS. Dr. Ronald Domitrovic is Program Manager and John Bush is a Senior Engineer at the Electric Power Research Institute (EPRI)
11、in Knoxville, TN. was modified such that each of the five circuits of the outdoor heat exchanger can be bypassed with hot gas coming from the compressor discharge line. Valves in each circuit allow for partial restriction of hot gas flow; this allows the remaining refrigerant (not used for hot gas b
12、ypass) to travel through the condenser and provide some heating capacity during defrosting. Numerous strategies of defrosting the outdoor unit by controlling defrosting order, flow rates, and refrigerant pressure drop were evaluated to understand the potential of the technology for residential and l
13、ight-commercial applications. This exploratory study found that the technique is effective, but not yet as efficient as conventional reverse-cycle defrosting. Several system improvements have been identified that may make this technology more efficient than conventional defrosting strategies. PROTOT
14、YPE SPECIFICATION A prototype system was constructed consisting of a small, commercially available residential heat pump system with several key modifications. The unit included a matching pair of indoor and outdoor units rated at 2.5 tons and a custom manifold system for hot gas bypass testing. Fig
15、ure 1 shows the prototype refrigerant flow diagram. As can be seen, each of the five circuits in the outdoor coil can allow hot gas to flow through from the discharge line. Metering valves before and after the outdoor coil allow for flow adjustments in each circuit. Instrumentation locations are den
16、oted in the drawing for all relevant measurements: Temperature (T), Pressure (P), refrigerant mass flow rate (), Power (W), and Relative Humidity (RH). Figure 1 Hot Gas Bypass Heat Pump Prototype Refrigerant Schematic Experimental Setup The prototype unit was installed in the laboratory with the out
17、door unit in an environmental chamber and the indoor unit in a closed-loop wind tunnel. The environmental chamber was used to maintain constant temperature (1 K / 1.8F) and relative humidity (1.5% RH) for the outdoor unit during testing. In order to provide repeatable and realistic conditions for th
18、e indoor unit, the unit was installed in a horizontal configuration in a closed-loop wind tunnel to provide a controlled air volume at constant temperature at the coil inlet. Testing procedures were designed to approximate the conditions prescribed by AHRI Standard 210/240 (AHRI 2008). Temperature a
19、nd humidity conditions were maintained as described in the H2 test condition from the standard. Air entering the indoor unit was maintained at 21.1C (70F) dry bulb and 10C (50F) wet bulb (20% RH). Humidity in the indoor loop was not strictly controlled since the indoor coil rejects sensible heat onl
20、y and humidity levels have a negligible impact. Conditions in the environmental chamber were controlled to assure that an ambient dry bulb temperature of 1.7C (35F) was maintained, and wet bulb temperature was kept as close to 0.6C (33F) (82% RH) as possible. Initial experiments were carried out by
21、operating the heat pump in heating mode under the conditions described above. The unit was first run under factory default defrost to establish a baseline. The amount of frost that accumulated on the outdoor coil face right before the reverse cycle defrost (RCD) was initiated was used as the signal
22、for when defrosting was needed for subsequent HGB tests. Each defrost strategy was evaluated until frost was visibly removed from the coil face. Frost was “measured” using visual inspection only, through the use of video cameras installed for the purposes of experimentation. Following this prelimina
23、ry investigation, several tests were conducted under repeatable conditions such that energy input and heating energy output could be compared over a fixed time period. These results provide insight into the overall energy-efficiency of the different defrosting strategies. Experimental Findings Table
24、 1 summarizes the results of the first eight tests. In these experiments, the factory defrosting strategy was compared to several different HGB defrosting strategies. The duration of defrosting time is recorded along with the approximate heating capacity (if any) provided during defrosting. The foll
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