REG NASA-LLIS-0391-1995 Lessons Learned - Galileo Spacecraft Safing Recovery Anomalies.pdf
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1、Lessons Learned Entry: 0391Lesson Info:a71 Lesson Number: 0391a71 Lesson Date: 1995-05-30a71 Submitting Organization: JPLa71 Submitted by: S.R. Tyler / J.O. BlosiuSubject: Galileo Spacecraft Safing Recovery Anomalies Abstract: The Galileo mission twice experienced difficulties with recovery from saf
2、ing errors due to a lack of a formal safing recovery plan and to software/documentation that had not been kept current on spacecraft states. Maintain and update an anomaly recovery plan, log spacecraft event updates, take care in reusing previously successful command packages, and identify nonstanda
3、rd ground system configurations.Description of Driving Event: Two Galileo Spacecraft anomalies occurred during the week of September 12, 1994. Several difficulties were encountered during the recovery from these anomalies.The first anomaly was a Data Bulk Unit Memory (DBUM) parity error on the Galil
4、eo Command and Data Subsystem (CDS). This nonprivileged error resulted in spacecraft safing but did not bring down either CDS string. In response to this anomaly, the flight team developed a special privileged command program to isolate the failed memory byte. Although this program was almost identi
5、cal to a recent successfully run program, it required a nonstandard ground system configuration for command translation. This configuration was not established, causing the second anomaly which brought down the CDS A-string and re-executed safing.During the recovery from this second safing, an exist
6、ing recovery file was left unchanged from a year earlier, even though the one-way light time had doubled. As a result, an inappropriate Telemetry Modulation Unit (TMU) modulation index command was uplinked, causing a short data outage.During both recovery efforts, it was believed that the system fau
7、lt protection associated with safing had turned off the High Voltage (HV) to the Heavy Ion Counter (HIC). In fact, a patch had been Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-implemented a year earlier, which prevented the fault protection from
8、turning off the HIC HV. A lack of proper configuration management along with an inadequate check of the spacecraft state created this confusion. Since a prolonged lack of HV to the HIC would permanently damage the HIC, the project was forced to consider a risky proposal to switch the HIC to the only
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