REG NASA-LLIS-6416-2012 Lessons Learned - SpaceWire Cable Fabrication and Installation.pdf
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1、 Public Lessons Learned Entry: 6416 Lesson Info: Lesson Number: 6416 Lesson Date: 2012-2-3 Submitting Organization: GRC Submitted by: Ralph Zerick Subject: SpaceWire Cable Fabrication and Installation Abstract: This lessons learned addresses handling, fabrication, integration and test issues identif
2、ied during the use of Gore SpaceWire cable, part number GSC-05-82730-00, size AWG26. This wire was used in flight hardware intended for deployment on the International Space Station. Specific problems experienced with this wire as well as recommendations to avoid similar problems are discussed herei
3、n. Description of Driving Event: Preparation and execution of CoNNeCT Comm Performance and TVAC System Level Testing involved Gore SpaceWire cable, one cable stopped functioning after the flight enclosure was shipped to the vibration lab in preparation for system level vibration testing. Another cab
4、le stopped functioning after it was installed in the flight hardware, however, it had passed all tests performed during fabrication. Lesson(s) Learned: Cable EFA517-001, SpaceWire Cable #3 This cable stopped functioning after the flight enclosure was shipped to the vibration lab in preparation for s
5、ystem level vibration testing. Prior to final tie wrap installation to secure all the internal cable bundles and the movement to the vibe lab this cable was functioning properly. After extensive trouble shooting at GRC indicated a probable short or open, the cable was taken to the Naval Research Lab
6、oratory in Washington DC for further evaluation. Time Domain Reflectometry tests identified the conductor and location in the cable where an intermittent short existed. Destructive Physical Analysis confirmed the location of the short. Lack of detailed instructions in the process plan resulted in th
7、e omission of shrink tubing around the wires for protection when the backshell was installed. The technician who had been assembling the SpaceWire cables was away and his replacement was not aware the shrink tubing had to be installed as part of the assembly process. It was also very apparent the ex
8、panded Teflon insulation on the individual wires was very soft and susceptible to damage under even very light point compression. Cable EFA518 -002, SpaceWire Cable #4 This cable stopped functioning after it was installed in the flight hardware. It had passed all functional tests during assembly. Af
9、ter extensive troubleshooting it was determined alcohol used during the post solder cleaning process was absorbed by the expanded Teflon insulation, wicked its way up the cable, caused an insulation breakdown, and ultimate failure of the cable. Lack of drawing detail on the cable assembly drawing sh
10、owing the Micro-D connector face in relation to a right angle backshell resulted to the connector being incorrectly oriented during assembly. Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-Figure 1: Connector side by side with a dime Figure 2: Wires
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