REG NASA-LLIS-1316-2002 Lessons Learned Mars Exploration Rover (MER) Pyrotechnic Test Damage (2002).pdf
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1、Lessons Learned Entry: 1316Lesson Info:a71 Lesson Number: 1316a71 Lesson Date: 2002-11-01a71 Submitting Organization: JPLa71 Submitted by: R. Welch/ D. OberhettingerSubject: Mars Exploration Rover (MER) Pyrotechnic Test Damage (2002) Abstract: Pyro pin puller parts were unexpectedly ejected with exp
2、losive force during a test of the Mars Exploration Rover dynamic test model.The lesson makes personnel safety recommendations for pyrotechnic tests, suggests limiting use of refurbished pyro devices, and calls for improved procedures and oversight during their refurbishment. Description of Driving E
3、vent: Parts were unexpectedly ejected with explosive force during a test of the Mars Exploration Rover (MER) dynamic test model (DTM), shown in Figure 1. The MER High Gain Antenna (HGA) pyrotechnic release mechanism was fired in order to assess the shock loading on adjacent Rover components. Two NAS
4、A standard initiators (NSIs) were mounted on the pin puller (Figure 2) that releases the HGA for deployment. When they were fired, the pin impacted the retaining cap of the puller housing, shearing the threads holding the aluminum cap to the aluminum housing (Figure 3). This caused both the pin and
5、cap to be ejected explosively from the back of the mechanism.Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-refer to D descriptionDThe device failure was attributed to shearing of the end cap and/or housing threads, also shown in Figure 3. It is pos
6、sible that thread damage occurred in the failed device during its initial firing in an earlier MER pyroshock test and/or during the refurbishment process. This device was refurbished by disassembly and ultrasonic cleaning, and was reassembled without a formal written procedure or mandatory QA inspec
7、tion. The design of the failed pin puller differs from that of the MER flight design, which uses a higher strength aluminum alloy for the housing and a stainless steel end cap.refer to D descriptionDThe ejected cap and pin ricocheted off the Pan Cam Mast Simulator and then gouged the concrete clean
8、room wall. Although only critical test personnel were present in the clean room during this Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-hazardous test and they complied with existing safety procedures, they were narrowly missed by these projectil
9、es. No one was injured, though the Pan Cam Mast Simulator suffered superficial damage. Also, this anomaly released combustion products, which damaged a strip heater on the HGA, requiring replacement of the heater.A failure of this nature during flight operations could lead to significant loss of mis
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