欢迎来到麦多课文档分享! | 帮助中心 海量文档,免费浏览,给你所需,享你所想!
麦多课文档分享
全部分类
  • 标准规范>
  • 教学课件>
  • 考试资料>
  • 办公文档>
  • 学术论文>
  • 行业资料>
  • 易语言源码>
  • ImageVerifierCode 换一换
    首页 麦多课文档分享 > 资源分类 > PDF文档下载
    分享到微信 分享到微博 分享到QQ空间

    REG NASA-LLIS-6056-2011 Lessons Learned - Liquid Oxygen (LO2) Purity Impacts Engine Performance.pdf

    • 资源ID:1019514       资源大小:59.44KB        全文页数:2页
    • 资源格式: PDF        下载积分:10000积分
    快捷下载 游客一键下载
    账号登录下载
    微信登录下载
    二维码
    微信扫一扫登录
    下载资源需要10000积分(如需开发票,请勿充值!)
    邮箱/手机:
    温馨提示:
    如需开发票,请勿充值!快捷下载时,用户名和密码都是您填写的邮箱或者手机号,方便查询和重复下载(系统自动生成)。
    如需开发票,请勿充值!如填写123,账号就是123,密码也是123。
    支付方式: 支付宝扫码支付    微信扫码支付   
    验证码:   换一换

    加入VIP,交流精品资源
     
    账号:
    密码:
    验证码:   换一换
      忘记密码?
        
    友情提示
    2、PDF文件下载后,可能会被浏览器默认打开,此种情况可以点击浏览器菜单,保存网页到桌面,就可以正常下载了。
    3、本站不支持迅雷下载,请使用电脑自带的IE浏览器,或者360浏览器、谷歌浏览器下载即可。
    4、本站资源下载后的文档和图纸-无水印,预览文档经过压缩,下载后原文更清晰。
    5、试题试卷类文档,如果标题没有明确说明有答案则都视为没有答案,请知晓。

    REG NASA-LLIS-6056-2011 Lessons Learned - Liquid Oxygen (LO2) Purity Impacts Engine Performance.pdf

    1、Public Lessons Learned Entry: 6056 Lesson Info: Lesson Number: 6056 Lesson Date: 2010-02-2 Submitting Organization: JSC Submitted by: Kristen Kinder Subject: Liquid Oxygen (LO2) Purity Impacts Engine Performance Abstract: STS-114 experienced a very low Fuel Bias which lead to an investigation regard

    2、ing possible causes. One item that was reviewed was the effect that LO2 purity would have on Space Shuttle Main Engine (SSME) performance. Investigation yielded large differences between LO2 purity requirements between Stennis Space Center (SSC) and Kennedy Space Center (KSC) and that LO2 purity was

    3、 not accounted for in overall performance predictions. It was also identified that the current LO2 purity requirements were not adequate with the use of Flight Derived Dispersions to protect for an abnormally low LO2 purity day. Description of Driving Event: STS-114 experienced a very low Fuel Bias

    4、which lead to an investigation regarding possible causes. The LO2 purity at SSC where the SSMEs are tested was found to be very different than the LO2 purity at KSC and not accounted for in performance predictions. In addition, the run tanks at SSC are pressurized with Gaseous Nitrogen (GN2) which i

    5、ntroduces more contaminant in the LO2. Actions taken: 1. LO2 purity requirements were tightened to guarantee adequate LO2 at KSC on day of launch. 2. Additional LO2 purity sampling was implemented to every flight instead of every six months to ensure adequate LO2 on day of launch. 3. Increased LO2 p

    6、rocurement requirements at KSC only. 4. Provisions were put in place to adjust APM on day of launch should we have lower than expected LO2 delivery (but still within procurement requirements). Lesson(s) Learned: 1. By ensuring adequate LO2 purity, the likelihood of an LO2 Level Cut Off (LLCO) was dr

    7、astically reduced due to off-nominal engine performance. 2. By knowing LO2 purity prior to launch, the ability to hold back APM to offset for a low LO2 purity day was also achieved. Recommendation(s): *TEST AS YOU FLY, FLY AS YOU TEST* 1. Would strongly recommend future LO2 based engine programs imp

    8、lement a method to sample LO2 purity in-line/in-run during engine acceptance testing to establish a baseline. 2. Would recommend future programs maintain a preflight measurement capability of LO2 purity to ensure adequate performance during flight. 3. Would recommend implementing LO2 purity requirem

    9、ents for both test and flight that are compatible and correct for any differences in pre-flight predictions. 4. Would recommend not pressurizing LO2 run tanks at SSC with GN2, this only worsens the purity of the LO2 in the stand. Instead consider pressurizing with GO2. Evidence of Recurrence Control

    10、 Effectiveness: Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-N/A Documents Related to Lesson: SE-S-0073, NASA Specification Fluid Procurement and Use Control Mission Directorate(s): Space Operations Additional Key Phrase(s): Launch support systems

    11、 Vehicle concepts Acquisition / procurement strategy and planning Cryogenic Systems Propulsion Level II/III requirements definition Additional Info: Project: Space Shuttle Program Approval Info: Approval Date: 2011-09-14 Approval Name: mbell Approval Organization: HQ Provided by IHSNot for ResaleNo reproduction or networking permitted without license from IHS-,-,-


    注意事项

    本文(REG NASA-LLIS-6056-2011 Lessons Learned - Liquid Oxygen (LO2) Purity Impacts Engine Performance.pdf)为本站会员(unhappyhay135)主动上传,麦多课文档分享仅提供信息存储空间,仅对用户上传内容的表现方式做保护处理,对上载内容本身不做任何修改或编辑。 若此文所含内容侵犯了您的版权或隐私,请立即通知麦多课文档分享(点击联系客服),我们立即给予删除!




    关于我们 - 网站声明 - 网站地图 - 资源地图 - 友情链接 - 网站客服 - 联系我们

    copyright@ 2008-2019 麦多课文库(www.mydoc123.com)网站版权所有
    备案/许可证编号:苏ICP备17064731号-1 

    收起
    展开